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Electrical System Drain

3174 Views 12 Replies 8 Participants Last post by  MicheleFrankie
I received my '22 Ford Lightning on 10/7/22. By that evening, I was receiving an error on the dash and via the Ford Pass App: "There is an electrical drain in '22 Lightning, pssibly caused by after-market device(s). If that's not the case, please schedule service soon." I only had the truck for 1/2 a day so no after market anything has been added.

I took the truck in and after 5 days of diagnostic work, they decided the "Gateway Module" was defective and needed to be replaced. Ford engineers were consulted during the process. The part is currently unavailable anywhere and on backorder with no anticipated delivery date.

I had them reassemble my brand new truck and said I would live the 2kWH drain per day until I could get a new module as they gave me no other options. However, during the process of working on the truck, the Frunk latch was damaged and now needs replacement. That new part appears to be available and should be in this week.

No one seems overly troubled by this turn of events and the priority of getting my truck fixed is uncertain at this point. I've owned the truck for 11 days with 7 of them in the shop and 2 of them with a Frunk alarm dinging anytime the truck moves.
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My truck has complained about an electrical drain once in a while ever since I put in my dashcam - no surprise there. Day before yesterday, it started doing it every time I turn on the truck. I removed the dashcam power taps and anything else I could find, but still no go. Sounds like it's time to make a service appointment...
TECH=23361 PERFORMED BCM SYSTEM SELF TEST B1616 RAN OASAS NO SSM OR TSB. GO TO WSM PINPOINT TEST C1 CHECK FOR AFTERMARKET ACCESSORIES
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NO GO TO C2 CHECK THE VEHICLES FOR A HIGH LOAD DRAW
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BATTERY DRAWS AT 8MIL-AMP OK WITH IN SPEC. NO GO TO C3 CHECK FOR CORRECT OPERATION SHORT SOAK
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The system is operating correctly at this time. The DTC may have been set due to high network traffic or an intermittent fault condition.
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HOOK UP BATTERY CHARGER, CHARGED AND TEST BATTERY FAILED. (DTC 4Q3 H4TC ACES F62AJ) REPLACED BATTERY RESET BMS SENSOR. RERUN SELF TEST PASSED.


I guess it's possible I had a bum 12 V battery, but it was a bit surprising to me. Here's hoping for a more reliable result going forward!
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